We
have not implemented Appendix K using ultrasonic flow measurement for feedwater
as of yet.
Our
Question(s)
1)
What are other plants goals/expectations for maintaining power level? (=/- MW or
goal); How easy is it to maintain?
Is there a band within which you operate?
Wolf Creek's rated
thermal power is 3565 MW. Operations is expected to maintain the plant
between 3563 and 3565, unless performing an evolution that could result in a
positive reactivity addition. It requires multiple small dilutions
(or borations at BOC) during the day to stay in the band. It is not
difficult to maintain.
2)
How is your secondary calculation performed? (Averaging Inputs, Instantaneous values,
combination) Is it a module
or program on you plant computer or is it an off-line routine?
The secondary calorimetric is a live calculation performed by the plant computer and is used as the primary indication of reactor power.
The calorimetric currently calculates once per minute and uses 1-minute averages for all inputs. We tried instantaneous calcs, but this caused power to fluctuate in a sinusoidal pattern (matching the sinusoidal oscillations of FW flow). 1-minute averages sufficiently dampen the FW reg valve oscillations.
That said, the 1-minute points still have a lot of scatter, so the operators use the 10-minute and 1-hour moving averages to determine whether they are in the operating band.
3) Are your temperature and flow transmitters set specifically for this calculation? (dampening or bias settings)
We have no special
instrument dampening or filtering for calorimetric
inputs.
4) Are any of your control loops (Feedwater) used in the secondary calorimetric calculation?
We use FW flow
(venturi dps), FW temperature, SG Pressure as the main
inputs.
5) Have you had any issues related to power swings or related to your secondary calorimetric?
Coming out of our last outage (Refuel 15, Fall of 2006) calorimetric power was fluctuating slightly more than in the previous cycle. We initially suspected issues with the new Feed Reg Valve controllers (upgraded in R15) or issues with Feed reg valve movement. It turned out to be a result of upper plenum anomaly fluctuations. These cause fluctuations in Thots, Steam Flow and Feed flow.
This cycle our fluctuations in the 1-minute calorimetric point were about +/- 10 Mw about nominal power at BOC. Last cycle, they were about +/-6 MW about nominal.
J.
E. Willett
"Only
those who will risk going too far can
possibly find out how far one can go."
T.S.
Eliot (1888-1965)
----------------------------------------------------
Joseph
E. Willett, P.E.
Principal
Reactor Engineer, Nuclear Operations
E-mail:
jwillett@oppd.com
OR Joseph_Willett@hotmail.com
Omaha
Public Power District
Phone:
P.O. Box
399
Mail
Station: FC-1-1 Plant
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